📄 Extracted Text (725 words)
From: Richard Kahn
To: Jeffrey Epstein <[email protected]>
Subject: Fwd: March Barge log
Date: Thu, 07 Mar 2019 20:43:42 +0000
strange that she is not sending to us and only upon request
thank you
Richard Kahn
HBRK Associates Inc.
New York NY 10022
tel
fa
cel
Begin forwarded message:
From: Stephanie Remington
Subject: Fwd: March Barge log
Date: March 7, 2019 at 3:15:25 PM EST
To: J <[email protected]> Richard Kahn
Forwarded message
From: Bill Hague
Date: Sun, Mar 3, 2019 at 8:17 PM
Subject March Barge lo
To: Michael Glidden alMillia>, mike
grysko t>
March Barge log
3-1 Friday
Head installed and engine started.
Fly to NY to inspect Bush Master.
3-2 Saturday
Snow hampers inspection of exterior.
Vessel sound but not Bristol. Plenty of system documentation. Systems have age, are not pretty, but are neat.
Fire fighting system is not tested by present owner.This system is reported to be a crash bilge pumping system
as well but remains untested. Upgraded propulsion controls reported and felt. Electronics reportedly functional.
It's a big vessel. It has a lot of systems. Reportedly the hydraulic controls need to have the flow control
EFTA01031008
increased to increase response time. Engines and generators appear neat and well maintained. In frame main
engine rebuilds reported performed while owned by the NCDOT.
Some exfoliation corrosion visible in the steering compartment.
Wiring and races show age but no visible sign of defect.
Insulation. Vessel built in 1976. It is assumed it is compliant with the 1975 ban on asbestos use.
HVAC is functional in galley and berthing areas. Galley equipment present and reported functional including
refrigeration and a big freezer.
Starboard engine muffler shows evidence of an exhaust leak. Rear anchor and mounting bracket starboard side,
removed but held by owner. Anchor windlass and cable appear good. Port fed side holds a deployable heavy
steel stabilizer pylon that reportedly has a new winch and controller to be installed. Main cargo deck has been
plated over with reportedly 1/2" steel plate for previous loose material transportation missions. Other
modifications have been made to bulwarks for utility. Cargo deck shows plenty of evidence of use, wear and
tear and also shows corrosion control efforts and good coating to prevent more wastage. (Not structural)
Sea trial Sunday AM
3-4 Sunday
Greatly improved weather. Inspected ramp, loading deck and all interior spaces forward and amidship.
Solid condition throughout but work needed on the paint or coatings due to damage from heat from exterior
plating work that was noted in inspection. Hatch doors on wing wall access at gate need work. Some interior
exfoliation was observed midship port side in Tank room. Sewage treatment system NFG , smells a bit and is
used only as a holding tank for waste.
Workshop is full of spare parts and electrical equipment too numerous to mention tools, grinders and painting
gear.
During sea trail gen 1 had a heating issue and gen 2 brought on line. Stbd main stalled at shift and had to be
restarted in the engine room. Vessel is strong and smooth underway.
No smoke when at operating temp.
With a two ton load of industrial refuse forward and a half load of fuel, BushMaster made 9 knots smoothly at
1600 rpm with a less than clean bottom. Very good for a 200 ton boat. It's nearly silent compared to the LSJ
Barge.
Spud deploy/recover system needs completion.
Fuel gauges have an electrical flutter that needs diagnosis.
Anchoring needs to be addressed. The original anchor and mounting is removed but available. Reinstall
Start and stop capability of all power producing equipment needs installed in pilot house.
Radar operation is questionable and should be considered NFG. Autopilot should be tested and all electronics,
including chart plotter should be confirmed compatible for communication and function.
Consideration should be given to changing the existing ramp cable hoist lifting system to one similar to the one
we made for the LSJ Barge. Additionally, with design and construction work, the rear ramp can be made to
allow rear, roll on capability wherever draft at the ramp is sufficient.
Conclusion.
This boat works. It needs upgrades and modification to be more ideal for our application but it's a worthy
candidate, and it's location is really handy.
Return flight canceled and rebooked due to weather. Newark/ Charlotte/St Thomas beginning 08:30 Monday.
Stephanie Remington
LSJE, LLC
EFTA01031009
ℹ️ Document Details
SHA-256
d9293dec22a6127c7962579a404b18723a8be2a966f1a85c7779969134a203ad
Bates Number
EFTA01031008
Dataset
DataSet-9
Document Type
document
Pages
2
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