📄 Extracted Text (283 words)
To: Brice Gordon
From: Jeffrey Epste n
Sent Sun 3/23/2014 12:51:09 PM
Subject Re: Dakota Well
yes
On Sun, Mar 23, 2014 at 6:50 AM, Brice Gordon wrote:
Jeffrey
After three failed attempts by HSG drillers to remove pump from the Dakota Well, I was able
get Rogers and Company to acid treat, pull pump with there large Rig- Friday last week.
Photo 1
Unfortunately they where unable to remove pump from well.
At this time the pump, 900 plus feet of 3 phase wire and the sounding tube are still in the well.
The pump separated from the discharge tube, Photo 2
Rogers feel it is completely stuck in the Well at set level of 1000 ft
If this is the case then the Dakota well will be most likely be non operational.
Casey Cook is recommending a Video camera be sent down to determine where the pump is.
If the pump has fallen to the bottom of the well, we maybe able to install a new pump, wire and
sounding tube
Cost $2061.36, attached estimate
Rogers could be here Monday.
Shall we proceed with Video
regards
Stanley, NM 87056
***********************************************************
The information contained in this communication is
confidential, may be attorney-client privileged, may
constitute inside information, and is intended only for
the use of the addressee. It is the property of
Jeffrey Epstein
EFTA_R1_00377900
EFTA01929067
Unauthorized use, disclosure or copying of this
communication or any part thereof is strictly prohibited
and may be unlawful. If you have received this
communication in error, please notify us immediately by
return e-mail or by e-mail to jeevacationegmail.com, and
destroy this communication and all copies thereof,
including all attachments. copyright -all rights reserved
EFTA_R1_00377901
EFTA01929068
ℹ️ Document Details
SHA-256
f0d1b06317c7376115fa5fb8ea2ef4ea0234cb85a5c3509727ecda06a116c27c
Bates Number
EFTA01929067
Dataset
DataSet-10
Document Type
document
Pages
2
Comments 0